Welcome Visitor. First time here? Like what you see? Bookmark us for when you are bored, and check out 'top shots' and 'fantastic (editors choice)' in the menu above, you won't be dissapointed. Join our community!
click here to sign up for an account today. Sick of this message? Get rid of it by
logging-in here.
M33131-16.
Thanks! Do you know why it was unusually late?
This probably won’t format properly… but here goes:
=== REPORTED DELAYS ===
MONHEADQU PQ – Browse – 23:23:03ET 3 >
Train Delay R Time Dl Description Sdiv Amount Equip/ Last Modified
Symbol Location G Lost Cd Of Delay Date Time Code No Hrs Mn Ticket id Failure Date/time Date Time User
———- —————– – —- — —————————————- ———- ——– —- —- —- —- ———– —————————- ———- ——– ——–
M 33131 16 PTROBI R 0100 OF LATE ARRIVAL OF 538 FROM CSXT BUFFALO 2015-06-16 11.43.00 OF 0307 1 2015-06-16 12.25.43 223316
M 33131 16 PTROBI R 0113 QT DRAWBAR FAILED ON GTW 126825 WHILE 2015-06-16 11.43.00 QT 0307 1 13 2015-06-16 12.31.01 223316
DOUBLING TRAIN. CAR SETOUT TO SERVICE
TRACK. WHILE PERFORMING AIR BRAKE TEST
OCPX 71761 DISCOVERED TO HAVE LEAKING
TRAIN LINE AND WAS SET OUT TO JC38.
M 33131 16 PARWES R 0020 TO CREW REPORTS EXCEEDED DESIGN TIME DUE TO 2015-06-16 16.39.00 TO 0304 20 2015-06-16 17.22.14 843721
BIG LIFT 36-3, RELEASE 10 HAND BRAKES
AND BRAKE TEST
Basically, L538 was late into Port Robinson with the traffic for M331 costing them an hour. B/O drawbar and B/O car cost them an additional hour. They also lost 20 minutes at Paris West making their lift.
Thanks for the info Tim!